Reject offboard


I did the procedures for calibration and I tried changing the knob for offboard but it says reject offboard.Is this an issue in the Q ground control or should I write a code in raspberry pi to make the autopilot work offboard.


It should NOT have ‘rejected offboard’. Did you have a good GPS Lock?
Please post the FlytOS runlog in this thread. Checkout this link to know more.


so there should be good gps lock . I think that is the problem.I will get back to you soon


I got a good GPS lock and I tried to run But it’s not working. I tried to run the offboard code it worked


can you please elaborate on what worked and what did not?

Also, what is printed on the screen, when you run python demoapp code.
Please share FlytOS runlog. Check this link to know more.