I did the procedures for calibration and I tried changing the knob for offboard but it says reject offboard.Is this an issue in the Q ground control or should I write a code in raspberry pi to make the autopilot work offboard.
It should NOT have ‘rejected offboard’. Did you have a good GPS Lock?
Please post the FlytOS runlog in this thread. Checkout this link to know more.
so there should be good gps lock . I think that is the problem.I will get back to you soon
I got a good GPS lock and I tried to run demoapp1.py. But it’s not working. I tried to run the offboard code it worked